I don't have any pictures of the belt, but let me tell you, it's not pretty. I went through a long trial an error process of getting the belt welded together properly so it wouldn't come apart under its own tension and getting it to the right length so that it didn't pull too hard on the motor but still had enough grip to spin the disc. I see now why some builders love this and others hate it.
With the new belt in place it was finally time for some testing. In drive testing I came to realize that the bot seemed sluggish. It was only upon further investigation that I learned that the built in mixing in my Spektrum Dx5e transmitter limits the fwd/rev channel to 70% of full throttle. Without time between now and the event to get a proper mixer it will have to do. Next was weapon testing, which went even worse than drive testing...